dcarver
Well-known member
So the thought crossed through the cranium scareabellium how wonderful KrZy8 was running.
JINX!
Yesterday, on commute, heard back firing on de-cel. Hmm.
..and mpg avg going from 44+ (unusually high)
..to 28 mpg (unusually low except if at go-to-jail-speed)
..and back and forth.
So, stopped by Chevron (my top-tier provider of choice), added 8.7 gallons to main and aux tank.
Purchased a bottle of 'Techron' and dumped all into the 6.6 gallon main tank.
Rode home, added SeaFoam, 3/4 bottle to Aux tank.
After just under 200 miles, (and mixing Aux tank SeaFoam with main tank Techron as the gauge dipped), she WAS running a *bit* better.
Main symptom? Transitioning off idle up to 3k rpm.
Idle, stable.
MPG - all over the place.
Firing misorder very evident from left bank, cylinders 1 or 2 as evidenced by placing hand at left exhaust. Can't be missed. Substanital.
Ok then.
Bike home, removed all plugs. All look good.
Removed fuel rail.
Going to replace injectors, 1, 2 with spares I have laying around.
Will replace 1, 2 sparking plugs too.
I care less about what's wrong than just
getting her fixed.
That is why I'm not an engineer... LOL.
Root Cause?
Good question.
My best hypostehsis is this-
My Aux Tank had an aluminum baffle cross-welded in on each quadrant. Only tack welded, which broke.
I attempted to fix by using JBWeld for gas.
Which broke free.
3 - 4 inch sections of JBWeld broke free after years of riding the dirt road back home.
The aluminum baffle plate, no longer secured, rotated to a postion where the JBWeld was rubbing against a section of the interior tank. The JBWeld was visibly reduced by the rubbing; from approx 5mm 'bead' to half that.
And all that JBWeld went somewhere.
I don't have a fuel filter between the aux tank and main tank.. but will have one by end of day tomorrow.
Will test the 2 injectors removed from KrZy8 tomorrow using a DIY homebrew method.
...and also test 2 injectors from the 'old' rail too.
Should be fun!
Later..
JINX!
Yesterday, on commute, heard back firing on de-cel. Hmm.
..and mpg avg going from 44+ (unusually high)
..to 28 mpg (unusually low except if at go-to-jail-speed)
..and back and forth.
So, stopped by Chevron (my top-tier provider of choice), added 8.7 gallons to main and aux tank.
Purchased a bottle of 'Techron' and dumped all into the 6.6 gallon main tank.
Rode home, added SeaFoam, 3/4 bottle to Aux tank.
After just under 200 miles, (and mixing Aux tank SeaFoam with main tank Techron as the gauge dipped), she WAS running a *bit* better.
Main symptom? Transitioning off idle up to 3k rpm.
Idle, stable.
MPG - all over the place.
Firing misorder very evident from left bank, cylinders 1 or 2 as evidenced by placing hand at left exhaust. Can't be missed. Substanital.
Ok then.
Bike home, removed all plugs. All look good.
Removed fuel rail.
Going to replace injectors, 1, 2 with spares I have laying around.
Will replace 1, 2 sparking plugs too.
I care less about what's wrong than just
getting her fixed.
That is why I'm not an engineer... LOL.
Root Cause?
Good question.
My best hypostehsis is this-
My Aux Tank had an aluminum baffle cross-welded in on each quadrant. Only tack welded, which broke.
I attempted to fix by using JBWeld for gas.
Which broke free.
3 - 4 inch sections of JBWeld broke free after years of riding the dirt road back home.
The aluminum baffle plate, no longer secured, rotated to a postion where the JBWeld was rubbing against a section of the interior tank. The JBWeld was visibly reduced by the rubbing; from approx 5mm 'bead' to half that.
And all that JBWeld went somewhere.
I don't have a fuel filter between the aux tank and main tank.. but will have one by end of day tomorrow.
Will test the 2 injectors removed from KrZy8 tomorrow using a DIY homebrew method.
...and also test 2 injectors from the 'old' rail too.
Should be fun!
Later..
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