There is no doubt that it was run with a dirty intake system, I used over two cans of carb cleaner to get the throttle bodies clean. After the oil in the cylinders, it ran but it was obviously low on power. I didn't do a compression test after running it, wish I had. The shop didn't do a compression test, they did a leakdown test. The best cylinder of the four had 20% leakage, one at 30%, one had 90% and another had 100%.
I guess it would have been interesting to try Ring Free or some other product and see how long I could have ridden this bike, but for $500 (shipped!) I got a really nice used engine with 35k miles. I thought about rebuilding the engine but I decided it would be too expensive.