Bike is buttoned up, cranks probably twice the RPM it had before. Gonna have some lunch, then go ride, get it warm, and come home to shut it off (just in case.)
Lost 15 minutes in reassembly because I had the airbox back in, then found the spring and washer for the idle adjustment screw, it was still disconnected from the throttle body. Had to take the airbox back out and take care of that. I hate being stupid! I wish it would stop.
Excellent news. Hoping the "hot test" goes as expected but I think the fact that the cold cranking speed is doubled says that you've found the smoking gun. ...or is that the deep throat? :blink:
Now, the next step is to take your old starter in to a electrical (starter) repair place and have them give it the once over. By the looks of yours, it should still be salvageable. I had a theory early on that got pushed aside that the magnet that came loose may have got banged around and lost some flux density. Trying to run a starter motor on ~ 3/4 of the field magnets is bound to make it run somewhat slow. I'm wondering if it could possibly be so easy.
You may be wondering if it is worth fixing the old starter. It will be to the next guy that needs one, and you can sell it to him.
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